Friday, 27 April 2018

27/4/18 - Pansy

Today I finished off the safety valve adjusting tool and did some tests on the valve.

Found a better result with a short hose directly onto the compressor rather than through the long hose and regulator. The plunger was skimmed several times and I think I might have gone past the critical setting as it was popping nicely in all cases but the shut down pressure isn't less than 7-10psi lower than the blow off pressure.

I have some more spindles and plungers to trial.

Happy steaming!

Nigel

Thursday, 26 April 2018

26/4/18 - Pansy

The test rig for the safety valve was made today from some plumbing pieces and a 3mm plate to clamp in the vise.

I made the nut and tail for the gauge as I didn't want to surrender one off this gauge and render it permanently assigned to the test rig. So while at it I beefed up the tiny little supply pipe so there's less chance of busting it off. The gauge sits on a nice ergonomic angle so no ungainly bending of the neck required for testing the valve :-)

Started making the adjusting spanner and then promptly lost the stainless pins I was making for it somewhere in the lathe! Wonderful to have such a clean machine but still couldn't find it! Ah well do it all again tomorrow!

Happy steaming!

Nigel

Wednesday, 25 April 2018

R class plates

A little while ago I had an order for a full sized R class number plate replica which I made from MDF, and also the North British Locomotive plate which is a copy the one belonging to R766. They were painted with enamels after sealing with primer and putty and look quite the part!

25/4/18 - Pansy

The safety valve body was drilled out and finished off with the seat tool.

The exterior body was profiled and tried with the shroud. Fits well. My final idea will have an O-ring to make the shroud a tighter fit on the valve so it doesn't come off so easily.

It was set up in the rotary table to mill the 1" hex on the base.

The plunger was made as are a couple of spares in the event too much is machined off the OD of the plunger. The aim is to achieve a minimal pressure drop between open and close and that is controlled by the diameter of the plunger.

The spindle and plunger were threaded a tight 3BA and silver soldered for security. The OD of the plunger was machined after soldering.

Happy steaming!

Nigel

Tuesday, 24 April 2018

24/4/18 - Lathe and back on to Pansy

Yesterday I rang the supplier of my lathe. They haven't continued this model for some time and the manufacturer in China has shut shop. They still have some spares but not in the way of bearings.

I've managed to locate some tapered roller bearings from the local bearing supplier as well as getting the rest of the headstock bearings quoted up.

Also I've fitted a rare earth magnet to the headstock sump to catch any metal moving through the oil. I got it from Jaycar.

The lathe service manager told me to tighten right up the preload on the spindle bearings to get me by for the time being. So that was done and some spirited running at 1500rpm for a while indicated yes they get warm but not hot. It's made a difference.

A check was made again in the headstock to see if the preload on the spindle had tightened up any of the other shafts. While at it I checked the rare earth magnet and it had done some good work picking up some metal. So hopefully we shouldn't be getting any such metal moving through the bearings again.

A series of test cuts were done and have satisfied myself enough for the present time.

So work turned again to the Pansy safety valve for a little while.

Happy steaming!

Nigel

Sunday, 22 April 2018

21/4/18 - Lathe!

The last few days have been flat out just fixing the lathe. I have had all the carriage in bits...long story but had the rack and pinion out of alignment with the bed and putting some downward pressure on the carriage. I've been chasing some "phonographing" which has turned up in the last few months on some of the cuts and suspected possible swarf under the carriage as a culprit giving it some springiness reflected in the cut.

Lots of work done. The rack dowel pins were holding the rack out of parallel...they were almost all removed and set up with a spacer block off the bed. A gasket added to the top of the apron gearbox to stop the pinion bottoming on the rack. Also noticed the fair share of paint and grit in the rack and pinion.

Swarf cleaned out of the apron which was coning from the cross slide area. Gearbox drained, and flushed.

The power feed shafts and lead screw were cleaned. Half nuts were jam packed with swarf.

The lathe was reassembled and a test cut done. There was a defiite improvement but still a small ripple on the cut.

The lathe was tried on several speeds and on low rpm with a lot of motor rattle the cut was horrible. Then turned off and disengaged the drive and wound by hand. Much better. So I realised that I had tightened up the belts and the tension and the way the motor supports on the head was introducing a lot of vibrations and harmonics...which would be much more evidenced if the spindle besring pre-load still wasn't enough.

Decision was made to inspect the spindle bearings so the head was dismantled enough to do that. I found that the main bearing behind the chuck had 3 brinells in it, but not able to be felt by hand. The outboard bearing looked worse and the rollers had skidded or somehow gotten some grooves possibly by something hard in there.

Also it was noticed the input shaft rumbles slightly.

So I thought a cleanup and flush of the bearings and a blow out with air might do for the moment...see how bad it is when there's no grit in the besrings with some more pre-load.

So the heastock was reassembled again with the same bearings with the plan to change the whole lot in the headstock at a future stage when I can see my way clear. The metal in the headstock oil even coming off the gears is something to be aware of.

The cut has definitely improved. The bearing pre-load cannot be underestimated, as also the much quieter operation with less tension on the belts.  I'll add a rare earth magnet into the bottom of the sump to pick up any other traces of metal floating around.

Happy steaming!

Nigel

Wednesday, 18 April 2018

17/4/18 - Pansy & lathe repair!!

The safety valve seat cutting tool was made and heat treated in oil. It was then tested successfully on brass and produced a good result.

My AL330a lathe which I bought almost 15 years ago has served me well but yesterday I noticed it has been producing some chatter marks even on finish cuts in the last few weeks, without any audible chatter. Faint marks but noticable. In machining the first cut on the outside body of the safety valve the depth of the chatter in waves was measured at 0.01mm and had approximately the same pitch as the carriage rack and the same number of ripples as the bearing rollers.

So the spindle bearings have been adjusted. Some seals are being replaced (leaks oil...finally have been able to trace where it comes from). The gear change levers had O-rings on the shafts and have found at least one was cut allowing oil to capillary past it. The O-ring grooves had razor sharp corners and they were chamfered to prevent it doing it again.

Grey flecks were noticed in the oil well and when the gear change levers were dismantled it was noticed they had drilled the dimples for grubscrews in the shafts and had left the swarf in the holes and jammed the grubscrews in!

I'm hoping the grey flecks in the oil well are leftovers from "running in" with the included bits of swarf coming from manufacture. The oil will be changed.

I had made the mistake of topping up with any thin motor oil over the last year rather than a hydraulic oil being a bit frustrated with the leaks becoming worse and not knowing where they were coming from and how much down time required to fix. As I learned yesterday the oil with detergents such as a motor oil holds particulate in suspension rather than a hydraulic oil letting it stay in the sump. I had typically used a gear oil previously and have a 20L drum of hydraulic so should be an easyish job to clean out and refill.

Some power feed shaft seals will be replaced as will the o-ring behind the bullseye sightglass as that was leaking too. I have found they are not a standard width but I can get narrower ones from a bearing supplier. The bullseye O-ring didn't have much chance as the spotface and threading operation left some burrs that had cut that one too.

Just goes to show the basic machine parts are probably fairly reasonable but as everyone tells me the Chinese lathes such as what I have has been put together in a hurry and has sharp burrs and could include swarf in the headstock. It would be a nuisance to strip down a brand new lathe but it might be worth the effort in the long run to not have cut seals and swarf where you don't want it.

Hopefully today (Wed 18/4/18) will be back in business with a repaired lathe.

Happy steaming!

Nigel

Monday, 16 April 2018

16/4/18 - Pansy

Some components have been made for the pop-type safety valve. My intention is to use an O-ring or two on the outside of the valve to hold the shroud on. Providing a little bit of stiffness to push on to prevent it rattling around on the painted cladding and also to accommodate for variations in squareness there.

Happy steaming!

Nigel

Wednesday, 11 April 2018

11/4/18 - Pansy

Today some work was done on the safety valve design, to fit the existing GWR shroud, and internals to be a "pop" type valve.  Warwick Allison's article in the AME magazine has been a very useful resource for the basis of this design.

Happy steaming!

Nigel

Tuesday, 10 April 2018

Friday, 6 April 2018

20/3/18 - 6/4/18 Pansy

I hope you had a great Easter break!  I have been sorting out a few other things requiring attention in the last couple of weeks but it's back to the work at hand.

Pansy passed its official boiler hydro test at the club to 200psi for 20 minutes..  I apologize for the photo rotation, no matter how many times I re-import it into the blog app, it remains turned horizontal!

Once back at the workshop, he regulator valve and internal steam plumbing and handle were fitted up to the boiler.  Some stainless steel studs were made for the regulator gland as well. Tank brackets on the smokebox are being modified to suit the shape of smokebox more correctly.

The cab bits are drawn up and I have several other things to get laser cut at the same time.


Happy steaming!

Nigel

Wednesday, 21 March 2018

14 - 20/3/18 Pansy

Over the last few days I have been joined in the shed by Paul who has come to have some working experience with me. He's learning how to paint some of our TrainAge signs which is a valuable service which we may be able to offer soon for the customers that order those.

On the locomotives, Pansy boiler is being prepped for a trip to the inspector to hopefully get approval to put it in the frames. The hydro test is done prior to fitment.

Happy steaming!

Nigel

Tuesday, 13 March 2018

8-13/3/18 - Pansy

A few days has been spent on straightening the running boards, adjusting bolt holes and tweaking the running board brackets, sorting out the sandboxes and bending their plumbing to represent the drawings more accurately. The running boards have been riveted too hard and had bowed. Also the brackets to the frame aren't all square or required a shim to get them to bolt up without huge tension on them causing them to bend out of shape again.

A few sand box bolt holes on one side of the frame were 7BA and required fasteners made, who knows why they were tapped oversize only on one side.

Another mystery was why the bolt holes in the running board brackets were mostly out of alignment witb the tapped holes in the frames. There's no other position it could sit in place and so was a womder how many screws were in the holes to begin with...maybe just a few. So the holes were filed into some slots to get the bolts to fit. One of those jobs where assembly and dismantling was every 5 minutes!

Happy steaming!

Nigel

Thursday, 1 March 2018

28/2/18 - Britt

The boiler was reinstalled back in the frame to begin looking at the regulator rods and positioning of the pivot on the boiler. Working off photos mainly. Using some 1/8" steel rod to set up some dummy rods and to see how close the handrail will come.

Happy steaming!

Nigel

Monday, 26 February 2018

26/2/18 - Britt

Today's work was to make the smokebox steam lance valve, bracket, and to extend the plumbing to it. The plumbing is quite visible behind the deflector so I couldn't really run it into space, and the valve is visible from the front. The plumbing comes from the tee piece below the whistle.

The bits were scaled off a couple of pictures and machined and silver soldered together. The bracket was made from 1/2" brass angle and heated and bent by hand to profile with the smokebox. The whole lot is secured by 10BA screws.

I have trialed the look of things with the existing smoke deflectors.

Happy steaming!

Nigel

Friday, 23 February 2018

23/2/18 - Britt

Plumbing for the whistle steam finished today. The bottom of the smokebox was drilled for a bulkhead elbow fitting I had made. The new plumbing nuts and tails made in house worked a treat. The plumbing was run insode the smokebox and to the whistle. The whistle is on an incline to automatically drain. It is placed between the frames under the smokebox saddle. The end of the whistle was already tapped 4BA and a plug was made to block it off so the whistle can sound.

The system was tested on air to prove it and it is very good. The whistle valve works well and looks the part.

Happy steaming

Nigel

Thursday, 22 February 2018

22/2/18 - Britt

Some more fittings were manufactured for the Britt smokebox. The plumbing union nuts were manufactured on my capstan lathe, instead of buying more in. I don't like fitting different style unions to plumbing (they vary between suppliers) so I have decided to make my own from now on. The union nuts will also suit other upcoming jobs so some extras were made while the machine was set up.

The capability of being able to produce my own stock for upcoming work using the capstan lathe has been a dream for the last few years since I bought the machine off a friend. It required an overhaul and adjustments and converting from 3 phase to single phase. That has been done over the last few years.

The common bits that seem to keep turning up so to speak are threaded nipples, plugs, nuts, basically anything repetative within the job that becomes hard to do with speed and efficiency on the centre lathe with any sort of volume. I was glad to be at the bottom of the box of plumbing nuts so I could use the machine to make some. Definitely Made in Australia. Very satisfying fitting these to the job and having some to spare for upcoming needs on the Britannia. A few more of the larger size will be made at a later stage when it comes to injector plumbing.

Happy steaming!

Nigel